diff options
author | Fam Zheng <famz@redhat.com> | 2014-05-21 10:42:13 +0800 |
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committer | Stefan Hajnoczi <stefanha@redhat.com> | 2014-05-28 14:28:46 +0200 |
commit | 271c0f68b4eae72691721243a1c37f46a3232d61 (patch) | |
tree | 70ea4e56b2f6705022b0c5979bb1564829d9dda6 /tests/qemu-iotests | |
parent | bd60436936ecebf2c683eef9ea561f2b949700f3 (diff) |
aio: Fix use-after-free in cancellation path
The current flow of canceling a thread from THREAD_ACTIVE state is:
1) Caller wants to cancel a request, so it calls thread_pool_cancel.
2) thread_pool_cancel waits on the conditional variable
elem->check_cancel.
3) The worker thread changes state to THREAD_DONE once the task is
done, and notifies elem->check_cancel to allow thread_pool_cancel
to continue execution, and signals the notifier (pool->notifier) to
allow callback function to be called later. But because of the
global mutex, the notifier won't get processed until step 4) and 5)
are done.
4) thread_pool_cancel continues, leaving the notifier signaled, it
just returns to caller.
5) Caller thinks the request is already canceled successfully, so it
releases any related data, such as freeing elem->common.opaque.
6) In the next main loop iteration, the notifier handler,
event_notifier_ready, is called. It finds the canceled thread in
THREAD_DONE state, so calls elem->common.cb, with an (likely)
dangling opaque pointer. This is a use-after-free.
Fix it by calling event_notifier_ready before leaving
thread_pool_cancel.
Test case update: This change will let cancel complete earlier than
test-thread-pool.c expects, so update the code to check this case: if
it's already done, done_cb sets .aiocb to NULL, skip calling
bdrv_aio_cancel on them.
Reported-by: Ulrich Obergfell <uobergfe@redhat.com>
Suggested-by: Paolo Bonzini <pbonzini@redhat.com>
Signed-off-by: Fam Zheng <famz@redhat.com>
Signed-off-by: Stefan Hajnoczi <stefanha@redhat.com>
Diffstat (limited to 'tests/qemu-iotests')
0 files changed, 0 insertions, 0 deletions